After the DSE601 pipe manual conversion my atomizer failed 2 days later. Coil burnt out on one side. The 601's are virtually impossible to clean so they have a very limited life expectancy.
As you can see in the picture it was heavily carboned matching the to 2 feed points.
I rebuilt the atty
without completely disassembling it. I soldered the wires to the new coil and fed it in from the top. To aid in soldering I electroplated the ends of the 36ga nichrome wire with copper. I built a "no wick" coil due to lack of materials. I've had attys that when cleaned had no wick and vaped very well. This one doesn't and will be getting a wick. I chatted with Carlos49 abt the silica wood stove rope he used.
This material looks very promising, but all I can find is the manufacturers site/description, No vendors. From the looks of the spool it may be hard to purchase just a 10' piece.
?High Temperature Insulation??alumina silica??colloidal silica??fiber materials??fiber silica??fused silica??high silica glass??high temperature cloth??high temperature fiber??high temperature silica??silica
I've seen it listed as small as 2mm dia. I might be able to strike a deal for 50-100' with the manufacturer. I'll send them an email and report back.
I plated the coil wire ends with copper (
Clean and Simple Electroplating ), wrapped the coil on a 1mm metal rod, soldered 30ga. enameled wire to it with a "hook & crimp" on each end. The bottom of the atty had a plastic disk glued in to remove and then I just probed with a needle to find the top layer of metal foam then peeled it back till the bottom of the ceramic cup was exposed. Removed the old coil and wires and fed the new one in from the top, on the form as far as I could. It actually went in easily if done slowly. Passing the one side under the bridge without deforming the coil is the worst part since both atty leads go into the cup on the same side of the bridge. After the coil is in place, bend the wires back up the outside of the atty band and tape them so the coil cannot move. Now put the 4 layers of the metal foam, disks with 2 holes in it, between the atty wires and fold the rest of the metal foam layers back down. The atty wires are now secure and the plastic disk can be slid on the atty wires and re-glued back into place. The failed circuit cooked the atty and melted the plastic disk cracking it in half.
This coil has more room to work than most I've seen.
I've considered making a plug in coil using IC socket connector pins. If the "cup" of the connector is to large, the connector can be drilled, using the cup hole as a guide, with a .005-.010 drill and pin vise from a jewelers set I have. The cup could be removed, the wire inserted in the pin, crimped, soldered and ready to plug in. The connectors plug in well to each other and can even be found gold plated. The cups could be glued to the bottom of the ceramic bowl as long as the metal foam isn't allowed to short them out.
Hope this will be of help to someone,
Vaporer