I finally got a stainless wick working well, heres what I did:
Switched to 30ga NiCr from 34ga. The heating characteristics are totally different, especially against stainless which sucks the heat.
2 x 5cm rectangle of 400 SS mesh.
Folded the mesh in half lengthwise so the cut edges get rolled into the center, leaving the smooth fold edge against the coil, eliminating the fringes of stainless fibers against the coil that cause hot spots and shorts.
11 wraps of 30ga (4.5" length wire) around a 6d finishing nail (3/32") gives me 2.5 ohms, great for the Vmax at 3 volts.
I oxidized the coil and mesh with a butane lighter only, cherry red for 10 seconds. Enough to burn off any manufacturing oils. Nothing crazy.
Installed coil to the screw and post using the nail in the well hole to keep it aligned.
Wick was rolled so It slid easily
throught the coil with enough friction so it won't slide out.
Drilled the fill hole to 3/32", chamfered and stuck in a 1cm piece of 3/32 o-ring as a stopper. No leaks.
Cut the bottom of the wick at a 45 degree angle. Trimmed the top of the wick 1/8 past the top knurled nut.
Align the air hole 15 degrees ahead of the wick so incoming air doesn't directly cool the coil.
For the first time I've been able to get clean/non-harsh/non-metalic volumes of vapor from a stainless wick.
Update: I just chain vaped through a full
tank, no problems. Wick got right to the last drop of
juice.
Update: 6 tankfulls later, simply amazing.